NICE3000 Motherboard Error Codes & Troubleshootings

Product
Error CodeError DescriptionFailure CauseMethodsGrade
Err02OvercurrentMain circuit output grounded or short-circuited.
Check if motor parameters have been tuned.
Load is too large.
Encoder signal is incorrect.
Verify if the UPS running feedback signal is normal
Check the output side of the controller to see if the contactor is operating normally.
Inspect the power lines for surface damage and the possibility of a ground short circuit. Ensure the connections are secure.
Check the motor-side terminal for copper wire grounding.
Inspect the motor internally for short circuits or grounding issues.
Check if the star contactor is causing a controller output short circuit.
Verify that the motor parameters match those on the nameplate.
Re-conduct motor parameter self-learning.
Check if the brake was continuously released before the fault occurred.
Inspect for any mechanical jamming.
Verify the balance coefficient.
Ensure the encoder-related wiring is correct and reliable.
For asynchronous motors, try open-loop operation and compare the current to determine if the encoder is functioning properly.
Check if the encoder’s pulses per revolution setting is correct.
Ensure the encoder signals are not interfered with.
Check if the encoder wiring is independently routed through conduits and if the routing distance is too long.
Verify if the shielding layer is grounded at one end only.
Ensure the encoder installation is reliable, and the rotating shaft is securely connected to the motor shaft, running smoothly at high speeds.
In non-UPS operating conditions, check if the UPS feedback is effective.
(Err02) Check if the acceleration and deceleration rates are too high.
5A
Err03Deceleration Overcurrent
Main circuit output grounding or short circuit
Whether the motor has been parameter-tuned
Load too large
Deceleration curve too steep
Incorrect encoder signal
5A
Err04Constant-speed OvercurrentThe main circuit output is grounded or short-circuited; the motor has undergone parameter tuning; the load is too large; the rotary encoder is subject to significant interference.5A
Err05OvercurrentInput voltage too high; Elevator counterweight serious; Brake resistor selection too large, or brake unit abnormal; Acceleration curve too steep;Adjust the input voltage; check if the bus voltage is normal and if it rises too quickly during operation; check the balance coefficient; choose the appropriate braking resistor; refer to the braking resistor recommended parameter table in Chapter 3 to ensure the resistance value is not too high; check if the braking resistor wiring is damaged, if there is any grounding phenomenon, and if the wiring is secure.5A
Err06Deceleration OvercurrentThe input voltage is too high; the braking resistor is selected too large, or the braking unit is faulty; the deceleration curve is too steep.5A
Err07Constant-speed OvercurrentThe input voltage is too high; the brake resistor is selected too large, or the brake unit is malfunctioning.5A
Err08Power-on buffer relay does not engage.
Maintenance reminder.
External power supply instability; hardware faults.
The elevator has not been powered off for maintenance within the specified time.
Confirm that the external power supply is stable and check that all power input terminals are securely connected; avoid powering the machine on again before it has been completely powered off; if hardware damage occurs, please contact the distributor or manufacturer. Perform maintenance or disable the F9-13 maintenance interval detection function.5A
   Err09   欠电压故障Instantaneous power outage; input voltage too low; drive control board malfunction.Eliminate external power supply issues: Ensure there are no power interruptions in operation; check if all power input lines are securely connected to the terminals; contact the dealer or manufacturer if necessary.    5A
Err10Drive OverloadBraking circuit malfunction; excessive load; encoder feedback signal status; motor parameters accuracy; check motor power lines.

Check the brake circuit and power supply: Reduce the load; verify the encoder feedback signal and settings; check if the initial angle of the synchronous motor encoder is correct; inspect the motor parameters and adjust them; check the motor-related power lines. (Refer to Err02 troubleshooting method)4A
Err11Motor OverloadImproper FC-02 setting; abnormal holding circuit; excessive load.Adjust the parameters to keep FC-02 as the default value; refer to Err10.3A
Err12input side phase lossInput power supply is asymmetrical; drive control board is abnormal.Check if the three-phase power on the input side is balanced and if the power supply voltage is normal; adjust the input power supply. Please contact the dealer or manufacturer.4A
Err13Output Side Missing PhaseLoose connection in the main circuit output;Motor damageCheck the wiring; inspect whether the output side contactor is functioning properly; eliminate motor faults.4A
Err14Module OverheatingHigh ambient temperature;
Fan malfunction
Blocked air duct
Lower the ambient temperature; clean the air duct; replace the fan; check if the installation space for the controller meets the requirements specified in Chapter 3.5A
Err15Output Side AbnormalitiesShort circuit in braking (resistor) output side
Operating contactor malfunction
Err16Current Control Faults1. Excessive deviation in excitation current;
2. Excessive deviation in torque current;
3. Exceeding torque limit time for too long
Input Voltage Low: Check the controller and motor connections.
Inspect the operation contactor.
Encoder Circuit Check: Inspect the encoder loop; check if the output circuit breaker is tripped; the current loop parameters may be too low; zero position might be incorrect, perform re-learning of the angle; load may be too high.
5A
Err17Encoder reference signal abnormalityDuring tuning, the Z signal arrives with a significant deviation from the absolute position.
During tuning, the UVW signals are abnormal.
Check if the encoder is functioning properly.
Check if the encoder wiring is secure and normal.
Check if the PG card wiring is correct.
Check if the grounding of the control cabinet and main unit is good.
5A
Err18Current Detection FaultDrive control board abnormalPlease contact the agent or manufacturer.5A
Err19    Err19Motor Tuning Failure1: Failure of stator resistance recognition 5, 6: Failure of pole position recognition 8: Retention 11: Failure of angle saving for angle-free learning of synchronous machine 101, 102: Motor tuning timeoutInput motor parameters correctly;
Check the motor leads and whether the output-side contactor is missing a phase;
Check the connections of the rotary encoder and confirm that the number of pulses per revolution is set correctly.
When tuning without load, check whether the brake is released.
When tuning a synchronous machine with load, ensure that the tuning is completed before releasing the maintenance operation button.
5A
Err20Speed Feedback Error FailureLoss of AB signal during identification process
Retain
Motor phase sequence reversed
Identification process cannot detect Z signal
SIN_COS encoder CD line disconnection
UVW encoder UVW line disconnection
Absolute position angle and cumulative angle deviation greater than 70 degrees
Overspeed or excessive speed deviation
SIN_COS encoder AB signal interference
SIN_COS encoder CD signal interference
Torque limit, speed measurement is 0
Loss of AB signal during operation
Loss of Z signal during operation
AB analog signal disconnection during low-speed operation
During tuning, CD signal error or severe interference with Z signa
Check if the Synchronizer F1-00/12/25 is set correctly.
Verify the encoder signal connections.
Inspect for any mechanical jamming during operation.
Ensure that the brake is released during operation.
Check the grounding and address any interference issues.
For angle anomalies, perform a re-learning procedure on the main unit.
Adjust the speed loop parameters.
Check if the brake is released.
If the motor fails to start during the slip test, activate the slip function on F3-24.
5A
Err21Maximum frequency less than rated frequencyCheck F0-06 and F1-04 for correctness
Err22Leveling signal abnormal101: The leveling signal is valid during the floor switching process. 102: The falling edge of the leveling signal is not detected from the elevator start to the floor switching process. 103: The deviation of the leveling out position is too large when the elevator is in automatic operation;101, 102: Please check whether the leveling and door zone sensors are working properly; check the verticality and depth of the leveling insert installation; check the leveling signal input point of the main control board; 103: Check whether there is any slippage of the wire rope.1A
Err23Motor short circuit fault to groundmotor-side ground fault
Err24RTC Clock Failure101: Control board clock information abnormal.101: Replace clock battery; replace main control board.3B
Err25Stored Data Exception101, 102, 103: Abnormalities in the stored data of the main control board.101, 102, 103: Please contact the agent or manufacturer.4A
Err26earthquake signal101: Seismic signal is valid and greater than 2S.101: Check whether the seismic input signal is consistent with the parameter setting of the main control board (normally open, normally closed).3B
Err29Seal Star Contactor Feedback Abnormal101, 102: Synchronized machine sealing star contactor feedback abnormal.101, 102: Check whether the feedback input signal status of the door seal contactor is correct (normally open or normally closed); check if the contactor and the corresponding feedback contacts are operating normally; check the circuit of the door seal contactor coil5A
Err30Abnormal elevator position.101, 102: In fast run mode or leveling run mode, if the operating time is greater than the minimum value of F9-02 and (FA-38+10), but the leveling signal remains unchanged.101, 102: Check whether the flat-level signal line connections are reliable, whether there is a possibility of grounding, or if there is a short circuit with other signals; check if the floor spacing is too large, causing excessive return to the flat level time; check the encoder circuit for any signal loss4A
Err31storage chip faultReplace motherboard
Err33Abnormal elevator speed101: Fast train running overspeed
102: Maintenance or well-ditch self-learning running overspeed
103: Free-running vehicle overspeed
104: Emergency running overspeed
105: Bit8 emergency running time protection of F6-45 is activated; running time exceeds 50 seconds reports timeout fault.
106: Control board test deviation too large
101: Confirm the correct use of the rotary encoder; check the motor nameplate parameter settings; re-tune the motor.
102: Try reducing the repair speed or re-tune the motor; malfunction of the repair signal during fast operation.
103: Check if the star function is effective.
104, 105: Check if the emergency power supply capacity matches; check if the emergency operation speed setting is correct.
106: Check the encoder wiring; check if the communication quality between the control board and the lower-layer SPI is good.
5A
Err34logical failureControl board redundancy check, logic exceptionPlease contact the agent or manufacturer5A
Err35anomaly in shaft self-learning data101: During self-learning startup, the current floor is not the lowest floor or the forced deceleration at the next level is ineffective.
102: During the shaft self-learning process, the maintenance switch is off.
103: Power-on check indicates that shaft self-learning has not been performed.
104: In distance control mode, the check indicates that shaft self-learning has not been performed during startup.
105: The elevator operation direction does not match the pulse change direction.
106, 107, 109: Abnormal pulse length detected by the upper and lower leveling sensors.
108, 110: Self-learning leveling signal has not changed for over 45 seconds.
111, 115: Stored floor height is less than 50 cm.
112: After self-learning, the current floor is not the highest floor.
113, 114: Pulse verification exception.
101: Check if the forced deceleration at the next level is effective; verify if the current floor F4-01 is the lowest floor.
102: Check if the elevator is in maintenance mode.
103, 104: Shaft self-learning needs to be performed.
105: Confirm if the elevator’s operation direction changes match the pulse changes of F4-03: Elevator going up should increase F4-03; elevator going down should decrease F4-03. If not consistent, adjust it to match using F2-10.
106, 107, 109: Incorrect settings for the leveling sensor’s normally open/closed; sensor signal is fluctuating. Check if the sensor plate is properly installed and if there is strong electrical interference.
108, 110: If the running time exceeds the protection time (F9-02) and the leveling signal is still not received, address the issue.
111, 115: If there are floors with a height less than 50 cm, enable the ultra-short floor function. If not, check the sensor plate installation for that floor or check the sensor itself.
112: The maximum floor setting (F6-00) is too low and does not match the actual condition.
113, 114: Check if the leveling sensor signal is normal and re-perform the shaft self-learning.
4C
Err36“Running contactor feedback abnormal”101: The running contactor is not outputting, but the running contactor feedback is valid.
102: The running contactor is outputting, but the running contactor feedback is invalid.
103: No load on the asynchronous output terminal.
104: Inconsistent status of the running contactor feedback check points.
105: The running contactor feedback is valid before the re-leveling start.
101, 102, 104, 105: Check if the contactor feedback contacts are functioning properly; confirm the feedback contact signal characteristics (normally open, normally closed).
103: Check if the output lines U, V, W of the integrated elevator controller are connected properly; check if the running contactor coil control circuit is functioning correctly.
5A
Err37           Brake contactor feedback abnormal101: The brake contactor output is inconsistent with the brake feedback status.
102: The status of the selected brake contactor feedback points is inconsistent.
103: The brake contactor output is inconsistent with the feedback status of brake detection switch 1.
104: The status of the selected brake detection switch 1 feedback point is inconsistent.
105: Before starting the operation and releasing the brake, the brake contactor feedback is valid.
106: The brake contactor output is inconsistent with the feedback status of brake detection switch 2.
107: The status of the selected brake detection switch 2 feedback point is inconsistent.
108: The brake contactor output is inconsistent with the feedback status of brake line 1 on the IO expansion board.
109: The brake contactor output is inconsistent with the feedback status of brake line 2 on the IO expansion board.
101-104, 106-108: Check if the brake coil and feedback contacts are correct; confirm the signal characteristics of the feedback contacts (normally open, normally closed); check if the brake contactor coil control circuit is functioning properly.
105: Check the brake contactor feedback signal.
5A
Err38Rotary encoder signal abnormal101: Pulse signal F4-03 remains unchanged for a time exceeding the value set in F1-13.
102: Motor descending, F4-03 increases.
103: Motor ascending, F4-03 decreases.
104: In distance control mode, open-loop operation is set.
105: Elevator descending, upper limit switch activated.
106: Elevator ascending, lower limit switch activated.
107: Elevator descending, speed change at the upper speed. Elevator ascending, speed change at the lower speed.
101: Confirm whether the rotary encoder is used correctly; confirm whether the brake is functioning normally.
102, 103: Check if system grounding and signal grounding are reliable; check if the wiring between the encoder and the PG card is correct. Modify the value of F2-10.
104: In distance control mode, open-loop operation is set (modify F0-00=1).
105, 106: Check the upper and lower limit switches.
107: Check the forced deceleration at both the upper and lower limits.
5A
Err39Motor overheating fault101: Motor overheat relay input is active and persists for a certain period101: Check if the thermal protection relay base is functioning properly. Check if the motor is used correctly and if it is damaged; improve the motor’s cooling conditions.3A
Err40Elevator operation time-outElevator operation time-outPlease check the parameters, or contact the agent or manufacturer to solve the problem;4B
Err41Safety circuit disconnected101: Safety circuit signal disconnected101: Check the status of each switch in the safety circuit; verify if the external power supply is correct; check if the safety circuit contactor operates correctly; inspect the characteristics of the safety feedback contact signals (normally open, normally closed).5A
Err42Door lock disconnected during operation101: Invalid door lock feedback during elevator operation101: Check if the hall and car door locks are connected properly; verify if the door lock contactor operates normally; inspect the characteristics of the door lock contactor feedback signals (normally open, normally closed); check if the external power supply is normal.5A
Err43Abnormal upper limit signal101: During the upward operation of the elevator, the upper limit signal is triggered101: Check the characteristics of the upper limit signal (normally open, normally closed); check whether the upper limit switch is making proper contact; if the limit switch is installed too low, it may also be triggered during normal operation at the end station.4C
Err44Lower Limit Signal Abnormal101: During the downward operation of the elevator, the lower limit signal is triggered101: Check the characteristics of the lower limit signal (normally open, normally closed); check whether the lower limit switch is making proper contact; if the limit switch is installed too high, it may also be triggered during normal operation at the end station.4C
Err45Forced Deceleration Switch Abnormal101: During shaft self-learning, the downward forced deceleration distance is insufficient.
102: During shaft self-learning, the upward forced deceleration distance is insufficient.
103: During normal operation, the forced deceleration position is abnormal.
104, 105: When first-level forced deceleration is active, the speed exceeds the elevator’s maximum operating speed.
106: During shaft self-learning, the signals for the upward and downward second-level forced deceleration are abnormal.
107: During shaft self-learning, the signals for the upward and downward third-level forced deceleration are abnormal.
101-103: Check the contact of the first-level deceleration switches (up and down); confirm the characteristics of the first-level deceleration signals (normally open, normally closed).
104, 105: Ensure that the installation distance for forced deceleration meets the deceleration requirements for this elevator speed.
106: Check the contact of the second-level deceleration switches (up and down); confirm the characteristics of the second-level deceleration signals (normally open, normally closed).
107: Check the contact of the third-level deceleration switches (up and down); confirm the characteristics of the third-level deceleration signals (normally open, normally closed).
4B
Err46anomaly in the releveling process“101: The leveling operation is ineffective; leveling signal is invalid.”
“102: The leveling speed exceeds 0.1 m/s.”
“103: During fast car operation startup, leveling status is valid and there is door seal feedback.”
“104: During leveling operation, no door seal feedback or lock signal is received 2 seconds after the door seal output.
101: Check if the leveling signal is normal; 102: Confirm whether the rotary encoder is used correctly; 103, 104: Check if the leveling sensor signal is normal; Check the door closure feedback input points (normally open, normally closed); Check the SCB-A board relays and wiring;2B
Err47door seal contactor anomaly101: During leveling or early door opening operation, if the door closure contactor output is continuous for 2 seconds but the door closure feedback is invalid or the door lock is disconnected;
102: During leveling or early door opening operation, if the door closure contactor has no output but the door closure feedback is valid for a continuous 2 seconds;
103: During leveling or early door opening operation, if the door closure contactor output time is greater than 15 seconds;
106: During leveling operation, if the door closure feedback is detected as valid before starting
101, 102, 106: Check the door closure contactor feedback input points (normally open, normally closed); Check if the door closure contactor operates normally;
103: Check if the leveling and re-leveling signals are normal; Check if the re-leveling speed setting is too low
2B
Err48Door opening failure101: The number of consecutive door openings not reaching the position exceeds the Fb-09 setting.101: Check if the door machine system is operating normally; Check if the car top control board is functioning correctly; Check if the door open position signal is accurate.5A
Err49
Elevator door closing failure
101: The number of consecutive door closures not reaching the position exceeds the Fb-09 setting.101: Check if the door machine system is operating normally; Check if the car top control board is functioning correctly; Check if the door lock operation is normal.5A
Err50Continuous loss of leveling signals101: 3 consecutive detections of leveling signal sticking 102: 3 consecutive detections of leveling signal lossa. Check whether there is any abnormality in the leveling and door sensors b. Check the insertion depth and verticality of the leveling plate c. Check the leveling signal input point of the main board d. Check whether there is any slippage of the wire rope
Err51CAN communication failure101: CAN communication with the roof board of the car does not receive correct data for a certain period of time.101: Check the communication cable connection; check the power supply of the control board on the roof of the car; check whether the 24V power supply of the integrated controller is normal; check whether there is strong electric interference with communication.1A
  Err52outbound communication failure101: Modbus communication with outbound calls does not receive correct data for a certain period of time.101: Check the communication cable connection; check whether the 24V power supply of the integrated controller is normal; check whether the address setting of the outcall control board is duplicated; check whether there is strong electric interference with communication.1A
Err53Door lock failure101: After 3 seconds of door open output, the door lock feedback signal is still valid.
102: Multiple door lock feedback signals are inconsistent, with a duration of more than 2 seconds.
103: Reserved.
104: High and low voltage door lock signals are inconsistent.
105: After 3 seconds of door open output, the low voltage door lock short-circuit signal on the control board is valid.
106: After 3 seconds of door open output, the high voltage door lock short-circuit signal on the control board is valid.
101, 105, 106: Check if the door lock circuit operation is normal; check if the door lock contactor feedback contacts are functioning properly; verify that the system received the door open position signal while the door lock signal is valid.
102: When detecting hall and car door lock signals separately, the hall and car door lock statuses are inconsistent.
104: When detecting high and low voltage door lock signals simultaneously, the main board receives the high and low voltage door lock signals with a time difference of more than 1.5 seconds.
E53 fault protection, subcode 104 requires power-off reset.
105, 106: Check if the door lock short-circuit circuit is shorted during door opening.
5A
Err54Troubleshooting start-up overcurrent102: During maintenance startup, the current exceeds 120% of the rated current.

a. Reduce the load
b. Check if the motor phase sequence UVW is correct
c. Disable the startup current detection function by setting FC-00 Bit1 to 1
Err55change-over stop failure101: When the elevator is operating automatically, the door on this floor does not reach the open position.

101: Check the door open position signal for this floor.1A
Err56elevator door opening and closing failure signals101: Door open position signal is valid during operation.
102: Door close position signal is invalid during operation.
103: Both door open and door close position signals are valid simultaneously.

Check the door open/close position signals. Verify if the F5-25 switch’s normally open and normally closed settings are correct.
Err57SPI communication failure101~102: SPI communication error, no correct data received from DSP for 2 seconds continuously; 103: Mismatch fault between the special machine’s mainboard and the lower layer101~102: Check if the connections between the control board and the drive board are correct.
103: Please contact the agent or manufacturer.
5A
Err58Position protection switch abnormal101: Forced deceleration with simultaneous disconnection of upper and lower limits.”
“102: Simultaneous disconnection of upper and lower limit feedback
Check whether the forced deceleration switch and limit switch have normally open or normally closed attributes, and whether these settings match the parameters on the main control board. Also, check if the forced deceleration switch and limit switch are malfunctioning4B
Err62Analog DisconnectCar top board or main control board analog input disconnectionCheck if the analog weight channel selection F5-36 is set correctly.
Check if the analog input wiring for the car top board or the main control board is correct and if there are any broken connections.
1A
Err63Main board, driver board, display board not boundSubcode 01: Display board not bound.
Subcode 02: Main board or drive board not bound.
01: Insert the display board to change the bound display board
02: Change
Err64Device No. Binding
Err65Accidental movement of the carAccidental movement of the carTo reset the fault, press the red button on the operator.
Err66Brake force detection faultsPulse input during brake force detectionCheck if the holding brake force is normal, adjust it a bit (F2-39), and then perform the brake force self-learning again
Err80Debug authorization code expires
Err81Temporary authorization code expires
Err83IoT without communicationsIoT module no communication for 5 minutesTurn on the IoT module to connect the IoT communication cable and antenna
Err84IoT without communication for a long timeIoT module no communication for over 45 daysTurn on the IoT module to connect the IoT communication cable and antenna
Err88Factory automatic test function

FP-09 for 0 non-protocol, 1 with protocols

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